渗滤液处理站升级改造方案研究与工艺设计
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杨超,金鑫,郭雨阁,金鹏康
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Schematic studies and process design for reconstruction of a leachate treatment station
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Chao YANG,Xin JIN,Yuge GUO,Pengkang JIN
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表2 升级改造工艺效果
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Table 2 Inlet and outlet water quality after reconstruction
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项目 | COD | BOD5 | NH4+-N | TN | TP | SS | 色度 |
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进水 | 4 023.1±50.29 | 864.2±23.16 | 338.5±12.83 | 402.1±19.98 | 10±0.21 | 732.8±34.95 | 200±9.44 | 固液分离出水 | 2 983.7±91.90 | 603.1±9.23 | 310.6±8.67 | 395.1±11.18 | 5.2±0.26 | 439.1±18.40 | 164±3.97 | 水解酸化出水 | 1 939.4±46.35 | 781.2±15.40 | 283.5±11.65 | 302.4±13.88 | 5±0.08 | 631.6±10.30 | 281±10.82 | MBR出水 | 263.6±5.77 | 62.1±0.76 | 19.2±0.93 | 31.3±0.85 | 0.5±0.01 | 1±0.04 | 80±3.34 | 臭氧气浮出水 | 153.1±2.05 | 26.3±1.28 | 18.8±0.54 | 30.2±1.40 | 0.5±0.01 | 1±0.01 | 20±0.37 | DTRO出水 | 56.7±1.13 | 14.6±0.48 | 16.4±0.60 | 28.2±0.65 | 0.1±0.00 | 0.2±0.01 | 10±0.12 |
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