某兰炭废水酚氨回收装置改造实践
武祝民, 李若征, 滕济林

Reformation practice of phenol-ammonia recovery unit for treating semi-coking wastewater
Zhumin WU, Ruozheng LI, Jilin TENG
表2 酚氨回收单元改造前后对比
Table 2 The comparison of the phenol-ammonia recovery unit before and after transformation
项目改造前改造后对比
出水水质COD/(mg·L-16 3772 265降低64%
总酚/(mg·L-11 693490降低71%
氨氮/(mg·L-13989增加128%
公用工程和药剂消耗电耗/(kW·h·m-32.52.2降低12%
低压蒸汽/(t·m-30.180.24增加33%
高压蒸汽/(t·m-30.030.08增加167%
循环水/(m³·m-3812增加50%
片碱/(kg·m-35.420.21降低96%
浓硫酸/(kg·m-34.370不消耗
溶剂/(kg·m-30.4100.146降低64%
副产品浓氨水质量分数10%~12%,产量5.3 L/m³质量分数16%,产量12.9 L/m³合格副产品,产生效益
粗酚含水率20%~30%,产量8.51 kg/m³含水率0.017%,产量9.78 kg/m³合格副产品,产生效益
综合运行成本63.00元/m³13.00元/m³降低79%
其他问题产生氨气逸散和硫酸钠废水无氨气逸散,无硫酸钠废水消除此问题