预臭氧+MBR+后臭氧工艺在焦化园区污水厂改造中的应用
李志雷, 刘宝富, 陈秀娟, 张德祥

Application of combined process pre ozone plus MBR and post ozone in sewage plant technical transformation project of coking park
Zhilei LI, Baofu LIU, Xiujuan CHEN, Dexiang ZHANG
表3 改造前主要运行成本
Table 3 Main operating costs before technical transformation
费用名称年使用量年费用/万元单位成本/(元·m-3
合计7.70
电耗4 833 600 kW·h338.351.03
气浮用PAC溶液(10%)657 t32.850.10
PAM(阴离子)6.57 t10.510.03
次氯酸钠(10%)328.5 t32.850.10
乙酸钠(25%)394.2 t59.130.18
工资福利费20人1200.37
粉末活性炭547.5 t4381.33
污泥危废处置费2 918.18 t1 459.094.44
脱水用PAC溶液(10%)583.64 t29.180.09
脱水用PAM(阳离子)3.5 t9.450.03
自来水费438 t0.150