预臭氧+MBR+后臭氧工艺在焦化园区污水厂改造中的应用
李志雷, 刘宝富, 陈秀娟, 张德祥

Application of combined process pre ozone plus MBR and post ozone in sewage plant technical transformation project of coking park
Zhilei LI, Baofu LIU, Xiujuan CHEN, Dexiang ZHANG
表6 改造后主要运行成本
Table 6 Main operating costs after technical transformation
费用名称数值单价/元年费用/万元单位成本/(元·m-3
合计4.73
电耗0.7 kW·h/a4 927 500344.931.05
气浮用PAC溶液(10%)657 t/a50032.850.10
PAM(阴离子)6.57 t/a16 00010.510.03
次氯酸钠(10%)328.5 t/a1 00032.850.10
乙酸钠(25%)394.2 t/a150059.130.18
工资福利费20人60 0001200.37
污泥处置费(危废)636.93 t/a5 000318.460.97
污泥处置费(一般固废)912.5 t/a20018.250.06
脱水用PAC溶液(10%)309.89 t/a50015.490.05
脱水用PAM(阳离子)1.86 t/a27 0005.020.02
液氧2 920 t/a1 0002920.89
自来水费438 t/a3.50.150.000 5
MBR膜更换费用10 640 m2/a120127.680.39
改造新增折旧费0.29
改造新增维修费0.25