INDUSTRIAL WATER TREATMENT ›› 2018, Vol. 38 ›› Issue (5): 54-57. doi: 10.11894/1005-829x.2018.38(5).054

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Research on the combined treatment of wastewater from rubber accelerant production

Zhang Yang1, Liu Yong1, Wang Hongping1,2   

  1. 1. School of Resources and Environmental Science, Wuhan University, Wuhan 430079, China;
    2. Hubei Provincial Collaborative Innovation Center for Water Resources Security, Wuhan 430072, China
  • Received:2018-02-14 Online:2018-05-20 Published:2018-05-29

橡胶促进剂生产废水联合处理工艺探究

张洋1, 刘勇1, 王红萍1,2   

  1. 1. 武汉大学资源与环境科学学院, 湖北武汉 430079;
    2. 水资源安全保障湖北省协同创新中心, 湖北武汉 430072
  • 通讯作者: 王红萍,副教授。E-mail:hongping.wang@whu.edu.cn。 E-mail:hongping.wang@whu.edu.cn
  • 作者简介:张洋(1993-),硕士。E-mail:whuzhangy@126.com。
  • 基金资助:
    湖北省环境保护专项资助项目(2011HB12)

Abstract: The wastewater from rubber accelerant production has been classified and collected. It is ascertained that the combined evaporation desalination-Fe-C micro-electrolysis-biochemical(activated sludge) process should be used for the treatment of this kind of wastewater. The results show that in the evaporation desalination stage,the eff-luent COD is only 3 112 mg/L,and the mass fraction of organic substances evaporated from salt 40%, when the evaporation capacity is 80%. In the Fe-C micro-electrolysis stage,the removing rate of COD is 31.15%,and B/C is increased to 0.303. Under the following conditions:reaction time is 4 h,pH value 3.5,and Fe/C ratio 2:1. In the biological (activated sludge) treatment stage,the effluent COD stabilizes at 100 mg/L and reaches the First-level national level of emission standard,the SOUR value of the activated sludge also stabilizes at about 45 mgO2/(gMLSS·h), after the sludge has been cultivated and domesticated for 32 days.

Key words: rubber accelerant wastewater, evaporation desalination, Fe-C micro-electrolysis, biochemical treatment

摘要: 对橡胶促进剂生产废水进行分类收集,确定了采用蒸发脱盐-Fe-C微电解-生化法联合的方法处理。试验结果表明,在蒸发脱盐阶段,蒸发量为80%时,出水COD仅为3 112 mg/L,蒸出来的盐中有机物质量分数达40%;在Fe-C微电解阶段,反应时间为4 h,废水pH为3.5,铁碳比为2∶1,COD的去除率可达31.15%,B/C可提高到0.303;生化处理(SBR工艺)阶段,对活性污泥进行培养和驯化32 d后,出水COD稳定在100 mg/L以下,达到国家一级排放标准,活性污泥SOUR也稳定在45 mgO2/(gMLSS·h)左右。

关键词: 橡胶促进剂废水, 蒸发脱盐, Fe-C微电解, 生化处理

CLC Number: