摘要: 在进水流量16.5 L/h,回流比200%,滤速2.8 m/h的工况下,考察了前置反硝化BAF工艺的处理效果。结果表明:在缺氧段与好氧段滤料体积比为1:1、1:2、1:3条件下,出水COD、NH3-N和TN均能达到《城镇污水处理厂污染物排放标准》(GB 18918—2002)的一级标准;在滤料体积比为1:4条件下,出水COD超出排放标准,而NH3-N和TN的出水效果仍满足一级排放标准。
关键词:
前置反硝化,
上向流曝气生物滤池,
缺氧,
好氧
Abstract: When the influent flow is 16.5 L/h, reflux ratio 200% and filtering velocity 2.8 m/h, the treatment effect of pre-denitrification BAF process has been investigated. The results manifest that when the filter volume ratios of anoxic section and aerobic section are 1:1, 1:2, and 1:3, its effluent COD, NH3-N and TN are able to reach the pri-mary Urban Sewage Treatment Plant Pollutant Discharge Standards(GB 18918—2002). When the filter volume ratio is 1:4, its effluent COD exceeds the discharge standard, but the effluent of NH3-N and TN still meets the requirements of priamry discharge standard.
Key words:
pre-denitrification,
upflow biological aerated filter(BAF),
anoxic,
aerobic
中图分类号:
汪荣, 杨卫东, 张有铭. 滤料体积比对前置反硝化BAF处理效果的影响研究[J]. 工业水处理, 2014, 34(7): 70-73.
Wang Rong, Yang Weidong, Zhang Youming. Study on the treatment effect of filter volume ratio on BAF pre-denitrification Wang Rong, Yang Weidong, Zhang Youming[J]. INDUSTRIAL WATER TREATMENT, 2014, 34(7): 70-73.