工业水处理 ›› 2014, Vol. 34 ›› Issue (7): 70-73. doi: 10.11894/1005-829x.2014.34(7).070

• 试验研究 • 上一篇    下一篇

滤料体积比对前置反硝化BAF处理效果的影响研究

汪荣, 杨卫东, 张有铭   

  1. 浙江欧美环境工程有限公司, 浙江湖州 313000
  • 收稿日期:2014-04-25 出版日期:2014-07-20 发布日期:2014-08-22
  • 作者简介:汪荣(1981-),研究生,工程师。电话:0572-2668888-8632,E-mail:RWang3@dow.com,wangrong1927@163.com

Study on the treatment effect of filter volume ratio on BAF pre-denitrification Wang Rong, Yang Weidong, Zhang Youming

Wang Rong, Yang Weidong, Zhang Youming   

  1. Zhejiang Omex Environmental Engineering Co., Ltd., Huzhou 313000, China
  • Received:2014-04-25 Online:2014-07-20 Published:2014-08-22

摘要: 在进水流量16.5 L/h,回流比200%,滤速2.8 m/h的工况下,考察了前置反硝化BAF工艺的处理效果。结果表明:在缺氧段与好氧段滤料体积比为1:1、1:2、1:3条件下,出水COD、NH3-N和TN均能达到《城镇污水处理厂污染物排放标准》(GB 18918—2002)的一级标准;在滤料体积比为1:4条件下,出水COD超出排放标准,而NH3-N和TN的出水效果仍满足一级排放标准。

关键词: 前置反硝化, 上向流曝气生物滤池, 缺氧, 好氧

Abstract: When the influent flow is 16.5 L/h, reflux ratio 200% and filtering velocity 2.8 m/h, the treatment effect of pre-denitrification BAF process has been investigated. The results manifest that when the filter volume ratios of anoxic section and aerobic section are 1:1, 1:2, and 1:3, its effluent COD, NH3-N and TN are able to reach the pri-mary Urban Sewage Treatment Plant Pollutant Discharge Standards(GB 18918—2002). When the filter volume ratio is 1:4, its effluent COD exceeds the discharge standard, but the effluent of NH3-N and TN still meets the requirements of priamry discharge standard.

Key words: pre-denitrification, upflow biological aerated filter(BAF), anoxic, aerobic

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