Abstract:
the research on the treatment project for denitrification mechanism of monosodium glutamate refining wastewater is introduced. A/O technological design has been used in the project. In the determination period,as the influent flux of the project is(1 270±335) m3/d,COD(1 724±897) mg/L,and TKN(93.5±41.5) mg/L,the effluent COD, TKN,and TN are (10.4±5.1),(0.6±0.4),and (7.2±1.5) mg/L,respectively. The average removing rates of COD,TKN and TN are 99.4%,99.4% and 91.7% respectively. It is obtained from the material balance that in the system,the denitrification capacity by anoxic denitrification is 56% of the total denitrification capacity,and the denitrification capacity by simultaneous nitrification-dentrification is 44% of the total denitrification capacity. Further research shows that high-efficient denitrification of the system is because the sludge has high denitrification activity in Tank A,and remarkable simultaneous nitrification-dentrification is occurs in the start part of Tank O.
Key words:
monosodium glutamate refining wastewater,
A/O process,
denitrification mechanisms,
simultaneous nitrification-dentrification
摘要: 文章研究了某味精精制废水处理工程的脱氮机理。该工程采用A/O工艺设计,实验测定期间,工程进水流量、COD、总凯氏氮(TKN)分别为(1 270±335)m3/d、(1 724±897)mg/L、(93.5±41.5)mg/L,出水COD、TKN、总氮(TN)分别为(10.4±5.1)、(0.6±0.4)、(7.2±1.5)mg/L,COD、TKN、TN平均去除率分别为99.4%、99.4%、91.7%。实验结果表明:系统高效脱氮是由于A池污泥反硝化活性高和O池前端发生了显著的同时硝化反硝化所致,分别占TN去除总量的56%和44%。
关键词:
味精精制废水,
A/O工艺,
脱氮机理,
同时硝化反硝化
CLC Number:
Zhou Sichen, Wang Yuan, Jin Xibiao. Research on the high-efficient denitrification mechanisms of monosodium glutamate refining wastewater by A/O process[J]. INDUSTRIAL WATER TREATMENT, 2018, 38(9): 79-82.
周思辰, 王远, 金锡标. A/O工艺对味精精制废水高效脱氮的机理研究[J]. 工业水处理, 2018, 38(9): 79-82.