工业水处理 ›› 2014, Vol. 34 ›› Issue (8): 36-40. doi: 10.11894/1005-829x.2014.34(8).036

• 试验研究 • 上一篇    下一篇

非均相催化臭氧化深度处理钻井废水的效能研究

袁建梅1, 杨德敏2,3,4   

  1. 1. 西南石油大学化学化工学院, 四川成都 610500;
    2. 国土资源部页岩气资源勘查重点实验室(重庆地质矿产研究院), 重庆 400042;
    3. 重庆市页岩气资源与勘查工程技术研究中心(重庆地质矿产研究院), 重庆 400042;
    4. 油气资源与探测国家重点实验室重庆页岩气研究中心, 重庆 400042
  • 收稿日期:2014-07-15 出版日期:2014-08-20 发布日期:2014-08-25
  • 通讯作者: 杨德敏,硕士,工程师。E-mail:yangdemin8628@163.com。 E-mail:yangdemin8628@163.com
  • 作者简介:袁建梅(1989-),在读硕士研究生。
  • 基金资助:

    重庆市应用开发科技项目(cstc2013yykfA20002);重庆市国土房管局重大科技攻关项目(CQGT-KJ-2012-6)

Efficiency research on the advanced treatment of drilling wastewater by heterogeneous catalytic ozonation

Yuan Jianmei1, Yang Demin2,3,4   

  1. 1. School of Chemistry and Chemical Engineering, Southwest Petroleum University, Chengdu 610500, China;
    2. Key Laboratory for Shale Gas Resource & Exploration, Division of Land and Resources, Chongqing Institute of Geology and Mineral Resources, Chongqing 400042, China;
    3. Chongqing Engineering Research Center for Shale Gas Resource & Exploration, Chongqing Institute of Geology and Mineral Resources, Chongqing 400042, China;
    4. Chongqing Shale Gas Research Center of State Key Laboratory of Petroleum Resource and Prospecting, Chongqing 400042, China
  • Received:2014-07-15 Online:2014-08-20 Published:2014-08-25

摘要:

采用单独臭氧氧化、MnO2吸附和O3/MnO2催化氧化3种体系对经过混凝处理后的钻井废水进行深度处理,重点研究了O3/MnO2催化氧化体系去除钻井废水中有机物(以COD计)的效能。结果表明:相比单独臭氧氧化和MnO2吸附体系,O3/MnO2催化氧化体系能显著提高COD和TOC的去除率;COD去除率随着臭氧投加量和催化剂投加量的增加、pH的升高和反应时间的增加而增大;在臭氧投加量为80 mg/L、pH为11.5、催化剂投加量为20 g/L、反应时间为40 min的最佳工艺条件下,COD和TOC的去除率分别达到87.51%、83.18%,COD从686.28 mg/L降至85.72 mg/L,出水达到《污水综合排放标准》(GB 8978-1996)的一级标准要求。

关键词: 非均相催化臭氧化, 钻井废水, 深度处理

Abstract:

Three kinds of systems,including individual ozonation,MnO2 adsorption and O3/MnO2 catalytic oxidation have been used for the advanced treatment of coagulation-treated drilling wastewater. The removing efficiency of organic matter(counted as COD) from drilling wastewater by O3/MnO2 catalytic oxidation process is studied emphatically. The results show that compared with individual ozonation system and MnO2 adsorption system,it is found that O3/MnO2 catalytic oxidation system can remarkably improve the removing rates of COD and TOC. The COD removing rate increases with the increase of ozone dosage and catalyst dosage,the rising of pH and lengthening of reaction time. Under the following optimum conditions:ozone dosage is 80 mg/L,pH 11.5,catalytic dosage 20 g/L,and reaction time 40 min, its COD and TOC removing rates are 87.51% and 83.18%,respectively. The concentration of COD declines from 686.28 mg/L to 85.72 mg/L. The effluent water quality could meet the first class of the Integrated Wastewater Discharge Standard(GB 8978-1996).

Key words: heterogeneous catalytic ozonation, drilling wastewater, advanced treatment

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