工业水处理 ›› 2021, Vol. 41 ›› Issue (12): 102-108. doi: 10.19965/j.cnki.iwt.2021-0297

• 试验研究 • 上一篇    下一篇

垃圾渗滤液DTRO浓缩液全量处理中试研究

张若砺1(),童兴明1,钟浩源2,杨金平3,许心武3,王新华1,4,*()   

  1. 1. 江南大学环境与土木工程学院, 江苏无锡 214122
    2. 四川宇科思通环保科技有限公司, 四川成都 641400
    3. 上海缘脉环境科技有限公司, 上海 201611
    4. 江苏省水处理技术与材料协同创新中心, 江苏苏州 215009
  • 收稿日期:2021-11-22 出版日期:2021-12-20 发布日期:2021-12-22
  • 通讯作者: 王新华 E-mail:877136290@qq.com;xhwang@jiangnan.edu.cn
  • 作者简介:张若砺(1996-), 硕士。电话: 18827278003, E-mail: 877136290@qq.com

A pilot-scale study on treating DTRO concentrate of landfill leachate

Ruoli ZHANG1(),Xingming TONG1,Haoyuan ZHONG2,Jinping YANG3,Xinwu XU3,Xinhua WANG1,4,*()   

  1. 1. School of Environment and Civil Engineering, Jiangnan University, Wuxi 214122, China
    2. Sichuan Yukesitong Environmental Technology Co., Ltd., Chengdu 641400, China
    3. Shanghai Yuanmai Environmental Technology Co., Ltd., Shanghai 201611, China
    4. Jiangsu Cooperative Innovation Center of Technology and Material of Water Treatment, Suzhou 215009, China
  • Received:2021-11-22 Online:2021-12-20 Published:2021-12-22
  • Contact: Xinhua WANG E-mail:877136290@qq.com;xhwang@jiangnan.edu.cn

摘要:

采用正渗透(FO)—低温蒸发—固化耦合工艺对垃圾渗滤液碟管式高压反渗透(DTRO)浓缩液进行全量处理的中试研究。结果表明,经过23 d的连续运行,中试装置的水回收率为64%,产水水质可满足《生活垃圾填埋场污染控制标准》(GB 16889—2008)表 2中排放标准要求;FO膜的平均运行通量为2.02 L/(m2·h),清洗周期为23 d;经过物理清洗和化学清洗后,FO膜的通量恢复率在95%以上,体现出较好的抗污染性能;固化产品的含水率 < 30%,满足运输和填埋要求。中试装置的处理规模为12 m3/d,总投资为300万元,运行成本为73.82元/m3。FO—低温蒸发—固化耦合工艺解决了垃圾渗滤液DTRO浓缩液的全量处理问题,在高盐废水处理领域具有较好的应用前景。

关键词: 正渗透, 垃圾渗滤液, DTRO浓缩液, 低温蒸发, 固化

Abstract:

A pilot study on the treatment of DTRO concentrate from landfill leachate was carried out using a combined process of forward osmosis(FO)-low temperature evaporation-solidification. The results showed that water recovery rate of pilot plant was 64% after 23 days of continuous operation, and the quality of effluent water could meet the discharge standard requirements in Table 2 of Standard for Pollution Control on the Landfill Site of Municipal Solid Waste(GB 16889—2008). The average operating flux of FO membrane was 2.02 L/(m2·h) with rinse period of 23 days. After physical and chemical cleaning, the flux recovery rate of FO membrane was above 95%, suggesting a better anti-pollution performance. The moisture content of the cured product was < 30%, which met the requirements of transportation and landfill. The treatment scale of pilot plant was 12 m3/d, with a total investment of 3 million RMB and an operating cost of 73.82 RMB/m3. The combined process achieved the purpose of total treatment of DTRO concentrate, which has a good application prospect in the field of high salinity wastewater treatment.

Key words: forward osmosis, landfill leachate, DTRO concentrate, low temperature evaporation, solidification

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