工业水处理 ›› 2024, Vol. 44 ›› Issue (1): 88-95. doi: 10.19965/j.cnki.iwt.2022-1278

• 试验研究 • 上一篇    下一篇

垃圾渗滤液的延时搅拌造粒混凝处理特性研究

钱朕1(), 何战友2, 金鹏康3(), 金鑫3, 宗宇凯1, 杨超1, 许兰洲3   

  1. 1. 西安建筑科技大学, 陕西 西安 710055
    2. 中国石油长庆油田分公司油气工艺研究院, 陕西 西安 710000
    3. 西安交通大学, 陕西 西安 710049
  • 收稿日期:2023-11-28 出版日期:2024-01-20 发布日期:2024-01-24
  • 作者简介:

    钱朕(1997— ),硕士。电话:19522509232,E-mail:

    金鹏康,教授。电话:0990-6633303,E-mail:

  • 基金资助:
    国家自然科学基金重点项目(52230001); 国家自然科学基金面上项目(52170052)

Treatment characteristics of the delayed stirring pelleting coagulation of landfill leachate

Zhen QIAN1(), Zhanyou HE2, Pengkang JIN3(), Xin JIN3, Yukai ZONG1, Chao YANG1, Lanzhou XU3   

  1. 1. Xi’an University of Architecture and Technology,Xi’an 710055,China
    2. Oil and Gas Technology Research Institute,Petrochina Changqing Oilfield Company,Xi’an 710000,China
    3. Xi’an Jiaotong University,Xi’an 710049,China
  • Received:2023-11-28 Online:2024-01-20 Published:2024-01-24

摘要:

混凝沉淀在垃圾渗滤液的深度处理工艺中是非常必要的预处理环节。传统的混凝工艺处理垃圾渗滤液普遍存在水资源回收率低、污染物去除率低、絮凝体松散等缺点。基于收缩脱水絮体致密化理论,提出了垃圾渗滤液的延时搅拌造粒工艺,通过长时间高强度的机械搅拌实现悬浮物的均一化。研究结果表明,在pH=12、搅拌强度为1 500 r/min、PAC和PAM投加量分别为3 000 mg/L和60 mg/L的最佳条件下,SS、浊度、COD的去除率分别可达92.33%、99.92%、35.84%。通过图像粒子测算系统测得最佳条件下絮凝体d 50为3.76 mm,沉速为20.08 mm/s,与常规混凝相比,沉速提升约60%。基于絮体沉速、投影面积、有效粒径等数据,计算得到三维分形维数为2.890 9,有效密度为0.087 6 g/cm3。延时搅拌造粒生成的絮体沉速快、密度大,混凝后的上清液回收率可由常规混凝的45%提升至85%。

关键词: 垃圾渗滤液, 延时搅拌造粒, 分形维数, 有效密度

Abstract:

Coagulation sedimentation is a critical pretreatment step in the advanced treatment of landfill leachate. Traditional coagulation processes for treating landfill leachate have drawbacks such as low water recovery,loose flocs,and low pollutant removal efficiency. A delayed stirring pelleting coagulation process of landfill leachate was put forwarded based on the theory of mechanical syneresis. Through long periods of high-intensity mechanical agitation,it could homogenize suspended solids. The results showed that the removal efficiency of SS,turbidity,and COD could reach 92.33%,99.92%,and 35.84% under optimal conditions of pH=12,stirring strength of 1 500 r/min,PAC and PAM dosage of 3 000 mg/L and 60 mg/L. The image particle measurement system revealed that under optimal conditions,the d 50 of floc was 3.76 mm and the sedimentation velocity was 20.08 mm/s,which was approximately 60% higher than that of conventional coagulation. According to the floc sedimentation rate,projection area and effective particle size,the three-dimensional fractal dimension was 2.890 9 and the effective density was 0.087 6 g/cm3. It was found that the floc produced by delayed stirring pelleting coagulation had fast sedimentation speed and high density,and the supernatant recovery rate after floc could increase from 45% conventional coagulation to 85%.

Key words: landfill leachate, delayed stirring pelleting coagulation, fractal dimension, effective density

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