工业水处理 ›› 2019, Vol. 39 ›› Issue (10): 97-99. doi: 10.11894/iwt.2019-0339

• 油气田水处理 • 上一篇    下一篇

一种高效反相破乳剂在胜利油田海洋采油厂的应用

荆波(),龚俊,郝明辉   

  1. 中海石油化工股份有限公司胜利油田分公司海洋采油厂, 山东东营 257237
  • 收稿日期:2019-06-21 出版日期:2019-10-20 发布日期:2019-10-29
  • 作者简介:荆波(1972-),硕士,高级工程师。电话:0546-8879277, E-mail:jingbo72@263.net

Application of an efficient reverse demulsifier in Offshore Oil Production Plant of Shengli Oilfield

Bo Jing(),Jun Gong,Minghui Hao   

  1. Offshore Oil Production Plant of Shengli Oilfield Branch of CNOOC Petrochemical Co., Ltd., Dongying 257237, China
  • Received:2019-06-21 Online:2019-10-20 Published:2019-10-29

摘要:

合成了一种高效反相破乳剂MH-9,并将其与破乳剂MC-9368配合使用处理采油污水。瓶试实验结果表明,当MH-9与MC-9368投加量分别为30、40 mg/L时,脱水率高达95.3%。中试实验结果表明,MH-9与MC-9368配合使用能够将三相分离器的水相出口含油量降低50%左右,同时将分水速率从200 m3/h提升到300 m3/h。该复合配方优化了平台集输系统,解决了陆地联合站高负荷海洋平台来液的问题,并且综合加药量低,环保,经济性好。

关键词: 海上油田, 反相破乳剂, 采油污水

Abstract:

A high-efficiency reverse demulsifier MH-9 was synthesized and used together with demulsifier MC-9368 to treat oil production wastewater. In the bottle test, when the dosages of reverse demulsifier and demulsifier were 30 mg/L and 40 mg/L, respectively, the dehydration rate was as high as 95.3%. In the pilot test of the Shengli Oilfield Marine Oil Production Plant, the oil content in the water outlet of the three-phase separator can be reduced by about 50%. Meanwhile, the water distribution rate increased from 200 m3/h to 300 m3/h. The platform gathering and transporting system is optimized, and the problem of liquid inflow from high-load offshore platform of land joint station is solved. The advantages of this product are low dosage, environmental protection and good economy.

Key words: offshore oil field, reverse demulsifier, produced water of oil field

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