工业水处理 ›› 2017, Vol. 37 ›› Issue (11): 87-88. doi: 10.11894/1005-829x.2017.37(11).087

• 油气田水处理 • 上一篇    下一篇

蓬莱19-3油田酸化返排液难处理原因探究

王国弘1, 王贺昌2, 王吉照2, 马浴铭2   

  1. 1. 中海石油(中国)有限公司蓬勃作业公司, 天津 300450;
    2. 中海油天津化工研究设计院有限公司, 天津 300131
  • 收稿日期:2017-09-26 出版日期:2017-11-20 发布日期:2017-12-21
  • 作者简介:王国弘(1971-),高级工程师。电话:022-66501500,E-mail:wanggh2@cnooc.com.cn。

Investigation on the cause of the difficulties of return acidizing fluids treatment in Penglai 19-3 Oilield

Wang Guohong1, Wang Hechang2, Wang Jizhao2, Ma Yuming2   

  1. 1. Pengbo Operation Co. of China National Offshore Oil Corp., Tianjin 300450, China;
    2. CenerTech Tianjin Chemical Research and Design Institute Co., Ltd., Tianjin 300131, China
  • Received:2017-09-26 Online:2017-11-20 Published:2017-12-21

摘要: 针对蓬莱19-3油田酸化返排液难处理问题展开研究,实验发现,该油田酸化返排液脱水困难,油相含水率偏高,乳化状态稳定。对可能导致返排液乳化稳定的物质进行了分离并鉴定,初步确定该物质主要成分为FeS。经验证,对除去FeS后的酸化返排液破乳,油水顺利分离。据此判定,导致蓬莱19-3油田酸化返排液乳化状态稳定且油水分离困难的物质主要为FeS。

关键词: 酸化返排液, 老化油, 油水分离, 乳化, FeS

Abstract: Aiming at the problem that return acidizing fluids of Penglai 19-3 Oilfield are difficult to be treated,according to the experimental results,it is found that the return acidizing fluids are characterized by difficult to be dehydrated,high oil phase watercontaining rate,and stable emulsion state. The substance that may lead to the stable emulsion state of return fluids has been separated and identified. It is preliminarily assured that the main component of the substance is FeS. The experience proves that after getting rid of FeS,the return acidizing fluids are demulsified, and the oil is separated from water favorably. The result decides that the substances which lead to the stable emulsion state of return acidizing fluids in Penglai 19-3 Oilfield and the difficulty of oil-water separation are mainly FeS.

Key words: return acidizing fluids, aging oil, oil-water separation, emulsion, ferrous sulfide

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