工业水处理 ›› 2009, Vol. 29 ›› Issue (11): 52-55. doi: 10.11894/1005-829x.2009.29(11).52

• 试验研究 • 上一篇    下一篇

反应与分离相耦合的钢铁酸洗液处理研究

马江权, 陈云国, 王岚   

  1. 江苏工业学院省精细石油化工重点实验室, 江苏常州 213164
  • 收稿日期:2009-07-20 出版日期:2009-11-20 发布日期:2010-10-01
  • 作者简介:马江权(1969- ),毕业于浙江大学,硕士,副教授,副院长。电话:0519-86330330,E-mail:majiangquan@em.jpu.edu.cn。
  • 基金资助:

    欧盟国际合作项目资助(EC Project BD Asia Pro Eco/07/96638);江苏省精细石油化工重点实验开放课题(KF0704)

Research on steel pickling wastewater treatment with membrane reactor coupling with membrane separation

Ma Jiangquan, Chen Yunguo, Wang Lan   

  1. Jiangsu Province Key Laboratory of Fine Petrochemical Engineering, Jiangsu Polytechnic University, Changzhou 213164, China
  • Received:2009-07-20 Online:2009-11-20 Published:2010-10-01

摘要:

采用反应与分离相耦合的途径,用19通道陶瓷膜元件构建了5L气升式膜反应器,并就其用于钢铁酸洗液的处理进行了研究。结果表明:在0.5~2.5m3/h曝气量范围内,稳定膜通量能维持在60L/(m2·h)以上,且提高曝气量有利于提高循环液体流速。在稳定操作条件下,料液中氢氧化铁悬浮物浓度、温度(1~45℃)和膜两侧压差(0.025~0.1MPa)均与膜通量呈线性关系。当处理Fe2+质量浓度为400mg/L的酸洗废液时,在溶氧度>70%、压差0.1MPa、18~25℃、pH为6~9、HRT=2h条件下,出水浊度2NTU,pH符合国家排放标准。

关键词: 多通道膜元件, 气升式反应器, 废水处理, 膜分离

Abstract:

Steel pickling waste has been treated by using a 5 L airlift membrane reactor which couples with a 19- channel porcelain membrane element.The results show that when the aeration volume is in the range of 0.5-2.5 m3/h, membrane flux can be maintained above 60 L/(m2·h).In addition,increasing the aeration amount is good for increasing the circulating liquid flux.Under stable operating conditions,the suspended solids concentration of ferric hydroxide in liquid,temperature(1-45 ℃) and operation pressure(0.025-0.1 MPa) show a linear relationship with membrane flux.Under the following conditions: Fe2+ mass concentration is 400 mg/L of pickling liquid waste,dissolved oxygen 70%,pressure difference 0.1 MPa,room temperature 18-25℃,pH 6-9,and the hydraulic retention time 2 h,the turbidity of effluent water is <2 NTU,pH accords with the national discharge standards.

Key words: multi-channel membrane elementairlift reactorwastewater treatment, membrane separation

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